Tuesday, November 18, 2008

Book reviews

http://www.jagclub.ru/triumph_news.html

Been involved in a fair bit of this, slow but steady and very exciting progress being made

Thursday, November 06, 2008

Shiney restored wheels on the herald




These K&N 6 x 13's were leaking and going flat due to salt induced corrosion so I cleaned/shotblasted and polished them then etch primed the hidden bits and clearcoated the polished bits... Herald is much happier now

Wednesday, November 05, 2008

More Exhaust comparisons

My mate Humph has a nice old Mk1 with a similar spec engine but until recently a botch up 6-3-1 exhaust built in the same manner as most currently on the market ie completely unequal lengths built in the that'll do manner...
The crap 6-3-1 = ~100rwhp from a 2.7PI


Mike the Pipe version ~ very good but not perfect ~ good for +18 bhp measured at the wheels




Anyway when he put his car on the same dyno it struggled to make 100rwhp and its power/torque curve was lumpy as hell.

After I fitted my new GT manifold and system I lent my old Mike Randell system to Humph to help him out.

Compare the results (red trace is the "proper" 6-3-1). As GT says , some exhaust are more equal than others








This is Humph on the dyno before any mods.... the fact that he got 118rwhp compared to 128rwhp I think is mostly down to him still running an 8 blade mechanical fan and the standard airbox



video

Tuesday, November 04, 2008

The quest for more bhp

This is a ongoing development program.. baseline testing was in July with the setup i have been running for about 4 years.
Untouched for weeks driven straight to the dyno with a tank of BP 98 she gave 128 rwhp and 172 lb/ft of torque after a couple of runs to clear the plugs


http://www.youtube.com/watch?v=hloGNgQfa-w&feature=channel

http://www.youtube.com/watch?v=W0xi_t9AExQ&feature=channel

I came back after 2 weeks and a bit of spannering with my new 6-3-1 but nothing else changed.





http://www.youtube.com/watch?v=mtlL1zR4omU&feature=channel

It ran the same topend power but had about 15% more torque from 2800 - 4500 rpm peaking at +190lb ft at just over 4000. After this it tailed back to the same top end power as previous


Work since then has included

1.Retiming the camshaft, Wade advise 102 deg (ie 3deg advanced) for the 444C 105 and it was at 108 so 6 degrees retarded over design. Think I installed it in error at 105deg +/- a degree and time and wear had retarded it further

That made a huge difference. Noticeably more "cammy" now and pulls with gusto through to plus 6000 whereas before it tailed off.

2. Adding 0.002" to the full load fueling to give 0.076"

3. Increasing fuel pressure to 130psi

4. Changed the dizzy to a solid state A123 billet job. Curve 7 - 10deg static 31deg max

Need to get back to the dyno asap to see what I have managed but seat of the pants testing says a big improvement